Posts about coding

Practice – January 20th

We drove the robot and looked at problems that were occurring. We fixed them by switching to a pulley system for the horizontal arm. After[…]

Practice – January 18th

Gavin worked on designing a new wheel-driven specimen grabber. Jordan worked on putting a DC motor on the existing claw to make it more stable.[…]

Practice – January 9th

We fixed some issues in coding, making the robot easier to handle during competition. For example, we switched our claw assembly to a locked position[…]

Practice – January 6

Documentation lost track of who did what. We did the following:

Practice – January 2

Michael coded the brush and vertical basket. Eric, Jordan, and Nick fixed and lubricated the vertical system. Preston continued with documentation.

Practice – December 2nd

We got the robot moving!!!!! Gavin worked on the vertical arm. Nick worked on making the horizontal grabber more compact. Eric worked on developing a[…]

Practice – December 30

Nick and Eric worked on attaching the collection basket to the vertical arm. Jordan and Carter worked on attaching the license plates to the robot.[…]

Practice – October 26

Preston worked on reducing the total cost of the Aerobotics Furniture Budget. Michael worked on implementing roadrunner as well as tested a lift arm. Nick[…]

Practice – October 7th

Michael made progress implementing RoadRunner into the robot. Gavin and Eric worked on CAD modeling the robot arms. Jordan and Kyle worked on a chain[…]

Sept 7, 2024 – Practice and Kickoff

Coders continued work on the acceleration/deceleration gain. Tried on jumpsuits for competition uniforms. Attended the 2024-2025 Into the Deep kickoff at Dayton STEM Academy.

Practice – September 2

Gavin worked on acceleration control for the robot. Joprdan and Eric worked on the extender arm. Preston worked on a budget for this year, as[…]

Practice – September 30

Preston worked on some logistical planning and began putting together a layout and budget for our workspace’s furniture. Gavin worked on 3D modeling the collector[…]

Practice June 29, 2024

Continued to create new autonomous test mode. Previous autonomous drive code was overwritten and must be recreated.

Practice – July 27

Gavin worked on coding distance driving for Autonomous. Eric worked on the extension mechanism for our experimental lifter arm. Preston researched newer components as well[…]

Practice – June 17

💡 Preston finished “coding” the MiniBot (Stephen did most of the work). 💡 Gavin, Michael, and Eric found a bad wire on the robot.

Practice – June 10

Gavin and Michael attended practice tonight. Laptops were being used by the Lego team, so limited programming available. Troubleshooting issues with receiving encoder values on[…]

Practice 5/25/2024

💡 Gavin worked on the coding the camera for the robot 💡 Jordan and Nick worked (unsuccessfully) on installing a latch for the hinging components[…]

Practice March 4th

Programming Fixed program to correctly use encoders and made a function that adds an acceleration to the beginning of the drive forwards. To slowly start[…]